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Part 1 – Experimental study of the pressure fluctuations on propeller turbine runner blades during steady-state operation

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Published under licence by IOP Publishing Ltd
, , Citation S Houde et al 2012 IOP Conf. Ser.: Earth Environ. Sci. 15 022004 DOI 10.1088/1755-1315/15/2/022004

1755-1315/15/2/022004

Abstract

A good evaluation of the unsteady pressure field on hydraulic turbine blades is critical in evaluating the turbine lifespan and its maintenance schedule. Low-head turbines such as Kaplan and Propeller, using a relatively low number of blades supported only at the hub, may also undergo significant deflections at the blade tips which will lead to higher amplitude vibration compared to Francis turbines. Furthermore, the precise evaluation of the unsteady pressure distribution on low-head turbines is still a challenge for computational fluid dynamics (CFD). Within the framework of an international research consortium on low-head turbines, a research project was instigated at the Hydraulic Machines Laboratory in Laval University (LAMH) to perform experimental measurements of the unsteady pressure field on propeller turbine model runner blades. The main objective of the project was to measure the pressure fluctuations on a wide band of frequencies, both in a blade-to-blade channel and on the pressure and suction side of the same blade, to provide validation data for CFD computations. To do so, a 32 channels telemetric data transmission system was used to extract the signal of 31 pressure transducers and two strain gages from the rotating part at an acquisition frequency of 5 KHz. The miniature piezoelectric pressure transducers were placed on two adjacent runner blades according to an estimated pressure distribution coming from flow simulations. Two suction sides and one pressure side were instrumented. The strain gages were mounted in full-bridge on both pressure and suction sides to measure the blade span wise deflection. In order to provide boundary conditions for flow simulations, the test bench conditions during the measurements were acquired. The measurements were made in different operating conditions ranging from part load, where a cavitating vortex occurs, to full load under different heads. The results enabled the identification and the quantification of the major known sources of pressure fluctuation as well as some unexpected ones. The paper first presents the experimental methodology discussing relevant topics such as telemetric system setup, transducers calibration and errors analysis. The main results are then presented to illustrate the relative amplitude of the main source of pressure fluctuations under different operating conditions. The discussion and conclusion addresses the important observations stemming from the data analysis and illustrates that most of the results can be correlated with the known behavior of hydraulic turbines while some require further investigation.

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10.1088/1755-1315/15/2/022004